by CREEKER69 »
Wed Dec 22, 2010 8:20 pm
Thank you, all, for the input. This Jukebox is a commercial (coin operated) version with Orange Rockola Amp and power supply, etc. The cabinet was made by Antique Apparatus Company. The production date is Oct of 2000.
I wish I was able to take a picture of the pilaster prior to my trimming of it. The curves and bubble view clear section were perfectly aligned but each end of the curved pilaster was, indeed, longer (wider) AND the overall height was about 3/8" taller. I was a little disappointed in that it was not a fit. To me, it was kind of like buying a new tail light lens for your car and being told to trim it so it fit.
But, at least Jorge (Rock-OLa (AA) parts/service man) did confirm this fact. There can be no way they are trimming them on the fly as they build them (At least I THINK they are still building them albeit different electronics). I also checked the part number in their manual for CD8 Bubblers that is posted online against the parts manual that was supplied with my 2000 version. Same part number, 57386-01. But, on to the trimming and if how worked or not.
It did work out. Jorge from AA-Rockola suggested Offset Aviation snips or Shear cutters to do the trimming. David (see post below) suggested a formica cutter or perhaps a table saw. Excellent suggestions. I had been thinking about doing the same thing. But instead, here is how I trimmed it. To determine how much to trim off each side, I placed the old pilaster inside the new one and held them together as tightly as i could without marring the inside surface of the new one and marked a pencil line along each side edge. That gave me the lines of each side to be trimmed.
Then, I placed the edge of the pilaster into my Black and Decker Workmate and clamped it so that I could just barely see the pencil line. Then I used one of those vibrating multi-function tools (like they sell at Harbor freight for 29.99) with the wide, rounded fine tooth blade. I held the blade flat on the work surface and gently and slowly ran it along the work surface, barely touching the pilaster that was clamped. It was like scoring it with the blade, but the blade actually cut deeper and if pushed would cut thru it.
I flipped it over and repeated the other side. I used a utility knife to carefully remove any burrs that may prohibit the edge from sliding into the narrow slot on the speaker side of the pilaster. Then I had to figure a way to do the top so I could shorten the pilaster.
There was no way I wanted to try freehand; I'm just not that good with a tool that vibrates to cut especially. Using the Workmate again, I clamped 3 wooden yard sticks down to the surface. These are the yard sticks available at Home Depot and are a perfect 1/4" thick (for like 60 cents each). I use them as fillers for wood working a lot.
I then had the lady of the house (this was the most dangerous part) hold the saw down on the top side of the yard sticks with about 1" of blade protruding over the edge and just hold it there steady. I stood the pilaster on its end and from the opposite side of the (the lower side of the surface since the yard sticks raised the saw blade), and I slowly moved the pilaster around the vibrating blade and trimmed the top edge. After cleaning it up with a utility knife, I went to do the install. It was just a little tighter than the one that came out but was not so tight as to give me pause to think of stress cracks, etc.
It really did not turn out to be all that bad, but I wish I hadn't had to do any of it. What causes those darn bubble tubes to burst, anyway? I took special care (Ron Rich's advice) when placing the bubble tubes back in. I made sure they were secure but had some slight movement ability. Sometimes when they forst start to bubble, they make a little banging noise like someone rolled a softball into the cabinet.
Thanks again to everyone and may everyone have a Merry Christmas (or Happy Holiday) and a Happy New Year.
Ron